Archive

  • 2023 Chill-Pro® Autumn Claims Highlights

    22-year-old Centrifugal chiller
    Cause of Loss: Oil Pump Failure

    DESCRIPTION: On date of loss, the oil pump failed on the referenced chiller causing the machine to go off on a safety failure. It was determined at that time that the pump and motor failed causing an over-amperage situation and tripped the safety on the machine. It was also determined at that time that the pump and motor were drawing too much amperage due to damaged windings and needed to be replaced to safely run the machine. Please note that the purge unit failed prior to the oil pump and was replaced. The oil pump was replaced new and the unit was returned to service.

    6-year-old Screw chiller
    Cause of Loss: Compressor motor windings shorted to ground

    DESCRIPTION: This was the initial loss for Compressor Number 2. The compressor shorted out in the motor windings. Initially, it was thought that the compressor had locked and later discovered when the old one was removed it turned freely. The compressor was replaced along with the contactor and fuses. After startup, everything was running normally. The oil separator height was 10 inches. It appears that the software on the Tracer interface for this chiller somehow got corrupted and the insured could not retrieve all the alarm history. The software issue has been corrected.

    9-year-old Magnetic Bearing chiller
    Cause of Loss: Loss of control voltage due to power surge

    DESCRIPTION: Called insured to discuss inverter damage to Chiller #2. Insured stated that the power surge in the local area caused loss of control voltage for Chillers Number 1 and 2. As a result, A/C D/C inverters had to be replaced on both chillers. No other damage noted to components other than control voltage.

    10-year-old Centrifugal chiller
    Cause of Loss: Circuit board failure

    DESCRIPTION: During the service call, the chiller was found to be inoperable. The troubleshooting procedure revealed failure of 4 printed circuit boards. Cause of failure unknown. Replaced circuit boards and restarted 450-ton Centrifugal Chiller. No further maintenance performed.

    2-year-old Centrifugal chiller
    Cause of Loss: Seized bearings, motor shorted to ground

    DESCRIPTION: Technicians found the chiller inoperable and pulling too many amps across the system. Testing of the single compressor on the chiller found that the compressor had seized bearings and would not turn. The seized bearings also caused the motor to burn up and short to ground. The compressor motor was then disconnected from the chiller and sent to be rebuilt. After the motor was rebuilt and returned to the loss site, technicians had the motor reinstalled. Vibration testing was completed and after a successful test, the compressor was restarted. After confirming no other problems with the compressor, the chiller was returned to service.

  • 2023 Chill-Pro Spring Claims Highlights

    10-year-old Centrifugal chiller. Cause of Loss: Variable Speed Drive failure.
    DESCRIPTION: Power module for 100 HP VFD Starter failed. Further investigation revealed two burnt
    spots in the power module. The cause of the burnt was electrical arcing in the power module. The main
    drive assembly was replaced, and the chiller unit returned to service. The unit was repaired and
    operational.


    14-year-old Magnetic Bearing, screw chiller. Cause of Loss: Magnetic bearing compressor failure.
    DESCRIPTION: Investigation revealed that on the date of loss – Turbocor Compressor Number 2 was
    operating at high output temperature. The unit was shut down and found that rotor magnetic bearing
    had failed. Turbocor compressor is not field repairable and requires replacement of the compressor. I
    have attached to this report a diagram of how the magnetic bearings are configured in the compressor.
    The manufacturer discounted the new compressor 32% after the core was returned. No other damage
    noted to chiller other than compressor failure.


    16-year-old air cooled Screw chiller. Cause of Loss: Screw compressor failed.
    DESCRIPTION: Compressor bearings failed causing compressor motor to seize. Replaced compressor,
    buss bars and fittings. Unit has been returned to service.


    9-year-old air cooled Scroll chiller. Cause of Loss: Scroll compressor failed.
    DESCRIPTION: Technicians were called out to the facility when the 210-Ton Scroll Chiller stopped working.
    Initial inspection found that one of the compressors on the chiller unit had stopped working. Further
    inspection of the compressor found that some of the contactors had welded closed. Due to the nature of
    the contactors welded closed, they could not simply be replaced, the entire compressor needed to be
    back to service.


    25-year-old Reciprocating chiller. Cause of Loss: Reciprocating compressor pistons failed.
    DESCRIPTION: Technicians were called to troubleshoot an issue with the 150-Ton Reciprocating chiller.
    Technicians discovered that the suction line for the compressor had broken, and refrigerant was leaking
    from the chiller unit. Technicians repaired the broken line and re-started the chiller.

    Within 4 hours of restarting, the suction line was broken again, and more refrigerant was lost. Technicians repaired the
    suction line to the chiller and restarted it. The technicians continued to monitor the compressor and
    suctions line. It was later revealed that the compressor attached to the recently repaired suction line was
    vibrating excessively. The vibrations caused another break in the suction line. Further investigation by
    the revealed that the compressor had broken pistons. The broken compressor pistons caused the unit to
    vibrate excessively causing damage to compressor suction line. A new compressor was installed, and the
    chiller system returned to service.

  • 2022 Chill-Pro® Summer Claims Highlights

    • 10-year-old, 120 Ton Air cooled Screw chiller. Cause of Loss: Drive rotor fused to compressor casing

    DESCRIPTION: Damage to Screw compressor while in operation. The male, or rotor driver, was found
    fused to the discharge wall of the compressor casing. The rotors were separated from the discharge wall
    during disassembly. Both the male and female rotors were found to be damaged. In addition to the
    damage found to the rotors, a significant amount of damage was also found on the discharge wall of the
    compressor. All thrust and counter thrust bearing appeared to be in good working order. The
    compressor required replacement as repair was not an option based on initial damage review.

    • 16-year-old, 500 Ton Centrifugal chiller. Cause of Loss: Ruptured O-Ring, refrigerant leak

    DESCRIPTION: 500 Ton Centrifugal Chiller had major leaks. Loss reported as major leak on chiller.
    Further communication with the insured revealed that an O-Ring blew out releasing an excessive amount
    of freon from the system. Contractor confirmed the damage to O-Ring. It appears that O-Ring was
    damaged and could not hold Freon in the system. The O-Ring was replaced, and Freon was added to the
    system. The bulk of claim cost was refrigerant recovery.

    • 15-year-old, 80-ton Scroll chiller. Cause of Loss: Electrical arcing, failed compressor

    DESCRIPTION: On date of loss, Technicians were called out when one of the six compressors on the 80-
    ton scroll chiller unit stopped working. Testing of the unit found that the compressor had shorted to
    ground. The compressor was replaced, and the unit was returned to service.

    • 10-year-old, 150 Ton Magnetic Bearing chiller. Cause of Loss: Stripped set screw, compromised seal

    DESCRIPTION: Our investigation found that on the date of loss, technicians were called out to diagnose a
    failure on the 150 Ton magnetic bearing chiller. Technicians found the system inoperable on a
    temperature alarm. Initial inspection found that the system had lost most of the refrigerant in the
    circuit, which caused the unit to overheat and force a shut down. Technicians traced the leak to a section
    of the line where a screw holding the sections together had been stripped out. Due to this section no
    longer being sealed properly, the refrigerant was released from the system. Technicians recovered the
    remaining refrigerant and repaired the section of the refrigerant line. They recharged the system with
    R134A refrigerant and re-started the chiller.

    • 10-year-old, 450 Ton Centrifugal chiller. Cause of Loss: Circuit board failure due to power surge

    DESCRIPTION: During service call chiller was found to be inoperable. Troubleshooting procedure
    revealed failure of 4 printed circuit boards. Replaced circuit boards and restarted 450-ton Centrifugal
    Chiller. No further maintenance performed.

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